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Date - 2. Purpose of the experiments. Experiments conducted to improve properties (solderability, cleanliness) of the connections of an electronic package. This package integrates in a single component every functions of the satellite calculator. Solder columns have been chosen as an example: som
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1. Experiments on Solder Column Interposer:cryogenic cleaning and local laser reflow
2. Date - 2 Purpose of the experiments Experiments conducted to improve properties (solderability, cleanliness) of the connections of an electronic package.
This package integrates in a single component every functions of the satellite calculator.
Solder columns have been chosen as an example: some of the following results derived from the experiments could apply to other types of connections (solder balls, leads…) or even boards
3. Date - 3 Solder Column Interposer (SCI)
the Solder Column Interposer (SCI) is made of a ceramic plate in which the array of solder columns are inserted. Basically, the attachment of SCI on the CLGA is made by reflowing eutectic solder bumps at the top of the SCI to form the package ready to be assembled in the end (CCGA for Ceramic Column Grid Array).
4. Date - 4 Assembly qualification Previous assembly qualification conducted in 2007 showed a poor reliability of solder columns. During the qualification test programme (vibration + shock + thermal cycling), large voids and cracks within the solder joints were noticed on external rows of the array of columns.
The occurrence of such defects lead to end the qualification earlier than expected.
5. Date - 5 Defects observed after investigations
Investigations carried out proved that columns were porous and that porosities may tend to propagate during tests within the solder joints to create the voids observed.
6. Date - 6 The study was broken down into 4 main steps:
SCI assembly on the CLGA
Improvement of SCI reliability
Package board assembly
Thermal cycling
7. Date - 7 Improvement of SCI reliability 2 major actions were performed to improve SCI reliability:
pollution removal by using a cryogenic cleaning method
solderability improvement and porosities mitigation by local laser reflow
8. Date - 8 Improvement of SCI reliability Pollution removal by cryogenic cleaning (technique developped by Air Liquide)
principle of cryogenic cleaning
projection of particles of dry ice on the surfaces to be cleaned
infra red thermocouple + electrostatic
fieldmeter utilized during the experiment
9. Date - 9 Improvement of SCI reliability Results after cryogenic cleaning
temperature ranged between -1 to 8°C
only 30 s is sufficient for cleaning
electrostatic charges can be generated during the process
surface roughness can be modified
Inspection under UV light: green spots indicates the presence of contaminants. More than 95% removed after cryogenic cleaning.
Good method to remove contaminants
10. Date - 10 Improvement of SCI reliability Results after cryogenic cleaning
left: before cleaning, right: after cleaning
surface roughness modified after processing
11. Date - 11 Improvement of SCI reliability Results after cryogenic cleaning
good results obtained, some improvements are necessary to be compliant with the electronic industry:
charge generation: air deionizer necessary to prevent charge generation
visual aspect after cleaning: impact of dry ice particles diameter on surface roughness to be optimized
12. Date - 12 Improvement of SCI reliability obtaining a smooth surface to regain a better solderability
13. Date - 13 Improvement of SCI reliability Local reflow of the end of the column by Laser reflow
14. Date - 14 Improvement of SCI reliability Results after Laser reflow
smooth surface obtained after Laser reflow.
Controlled reflow that keeps the geometry of the columns after process.
15. Date - 15 Improvement of SCI reliability Results after Laser reflow
smooth surface obtained after Laser reflow.
Controlled reflow that keeps the geometry of the columns after process.
16. Date - 16 Improvement of SCI reliability Solderability test
1 Part subjected to solderability testing after cryogenic + Laser reflow.
Reference standard: NF-A-89400
dip test
flux used: C25D (RMA)
immersion time = 5s
temperature of solder bath = 235°C
measurement of the contact angle ?
measurement of the force F
visual inspection
17. Date - 17 Improvement of SCI reliability Results after solderability test
not good according to the standard (slow wetting) but correct from an optical point of view (height of wetting area greater than the immersion depth) and better than previous solderability tests performed in the past (with regards to the height of wetting area)
18. Date - 18 Board assembly 3 parts were assembled on board:
1 part not processed
1 part subjected to cryogenic cleaning and Laser reflow
1 part subjected to Laser reflow (not polluted by contaminants)
Parts subjected to 500 Thermal Cycles (-55/100°C)
assembly after Laser reflow
19. Date - 19 Results after 500 Thermal cycles same behaviour for the 3 parts
cracks within the solder joints (left picture) & solder shrinkage (right)
20. Date - 20 Cross section after 500 Thermal cycles
part not processed (left). Laser processed (right)
21. Date - 21 Conclusion
The attempt to improve the SCI reliability failed; the same behaviour as during the first assembly qualification was observed (void, cracks within the solder joints).