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What’s This HWA Design Thing All About???. Design Capacity HWA Info from one POTW CITY OF GREENSBORO North Buffalo POTW. NORTH BUFFALO POTW. Design Flow: 16 MGD Current Flow = ~10.0 MGD Primary Treatment Secondary Treatment Trickling Filters Activated Sludge with Nitrification
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What’s This HWA Design Thing All About??? Design Capacity HWA Info from one POTW CITY OF GREENSBORO North Buffalo POTW
NORTH BUFFALO POTW • Design Flow: 16 MGD • Current Flow = ~10.0 MGD • Primary Treatment • Secondary Treatment • Trickling Filters • Activated Sludge with Nitrification • Tertiary Treatment • Phosphorus removal • Chemical Addition/Precipitation • Effluent Sand Filters
NB CURRENT MAHL CALCULATIONCBOD [Actual Removal/Actual Flow] NPDES Permit Limit: 8.0 mg/l (summer) Removal Rate: 98.8% (270 data points/MRE) Actual Flow: 14.2 MGD** 8.0 mg/l = 8.0 = 666 mg/l max. allowable 1.0-.988 .012 influent conc. 666 * 8.34 * 14.2 MGD = 78,952 pounds **DWQ required use of actual flow..flow has dropped since then. These are the approved headworks calculations from December 2003
“DESIGN CRITERIA”NORTH BUFFALO POTW • From Hazen and Sawyer Engineers Original Design (~1980 Upgrade) • BOD = 196 mg/l • TSS = 245 mg/l • Total Phosphorus = 6.0 mg/l • NH3-N = 18.5 mg/l
NB “DESIGN CRITERIA” per DWQMAHL CALCULATION: CBOD • Engineering Design BOD = 196 mg/l • Used BOD as CBOD • Engineering Design Flow = 16 MGD 196 * 8.34 * 16.0 = 26,154 pounds MAHL • Current Domestic BOD Loading: 27,615 lbs • 20 of last 24 monthly average influent concentrations exceeded 196 mg/l while resulting in average effluent CBOD of <2 mg/l • CAN YOU SPELL OVERALLOCATED?????
NB CURRENT HWA CALCULATIONTSS [Actual Removal/Actual Flow] NPDES Permit Limit: 30.0 mg/l Removal Rate: 97.8% (271 data points/MRE) Actual Flow: 14.2 MGD 30.0 mg/l = 30.0 = 1363 mg/l max. allow. 1.0 -.978 .022 influent conc. 1363 * 8.34 * 14.2 MGD = 161,492 pounds **DWQ required use of actual flow..flow has dropped since then. These are the approved headworks calculations from December 2003
NB “DESIGN CRITERIA”CALCULATIONS: TSS • Engineering Design TSS = 245 mg/l • Engineering Design Flow = 16 MGD 245 * 8.34 * 16.0 = 32,693 pounds [Current Domestic TSS Loading: 22,289] • Not overallocated now, but flow is only ~10.0 MGD • Domestic alone will use up the rest of the allocation
IMPLICATIONS • Underestimating POTW Conventional Pollutant Capacities and Capabilities • Potential Over-Allocation With Just Domestic Loading! • Loss of Potential New Industrial Users • Potential Moratorium • “Domestic concentration” is rising due to newer plumbing fixtures • BOD Limits for All SIUs • North Carolina Local Limits Policy
North BuffaloCurrent Loading Situation: DISMAL • Actual Influent CBOD Loading = 19,718 lbs • 213 mg/l * 8.34 * 11.1 MGD [24 mo. avg] • DWQ Design Loading = 26,154 lbs • 6436 lbs CBOD left…[“domestic” on paper is >MAHL] • BOD Limits for Everyone!!!! [75.4% “loaded”] • Actual Influent TSS Loading = 32,401 lbs • 350 * 8.34 * 11.1 MGD [24 mo. avg] • DWQ Design Loading = 32,693 lbs • Only 292 Pounds of TSS Left…but over 4 MGD of hydraulic capacity left… • TSS Limits for Everyone!!!! [~100% “loaded”]