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HSO SORPTION COOLERS Lionel DUBAND L. Clerc, D. Communal, M. Dubois (BV), JL. Durand, E. Ercolani, L. Guillemet, N. Luchier, L. Miquet, R. Vallcorba Service des Basses Températures CEA-SBT (CEA/DSM/DRFMC/SBT). MODELS - GENERAL STATUS. STRUCTURAL MODEL (STM). • No thermal capabilities
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HSO SORPTION COOLERSLionel DUBAND L. Clerc, D. Communal, M. Dubois (BV), JL. Durand, E. Ercolani, L. Guillemet, N. Luchier, L. Miquet, R. Vallcorba Service des Basses Températures CEA-SBT (CEA/DSM/DRFMC/SBT)
STRUCTURAL MODEL (STM) • • No thermal capabilities • • Main goal : validation of Kevlar suspension system • • Dummy cooler heart made out of aluminum • (was not intended to be • vibration tested cold)
VIBRATION TESTS - STM WITH KEVLAR 0.5 and 0.3 mm KEVLAR FAILURE Sinus [0 - 100 Hz] X : 40 G Y, Z : 25 G Random [0 - 2000 Hz] X : 14 G rms Y : 11.3 G rms Z : 9.9 G rms Visual inspection : rupture of one "stitch" CSL ROOM TEMPERATURE TESTS high G level Lateral motion Rubbing & rupture Analysis : Note : lowest resonant frequency > 450 Hz Kevlar 34 Replaced by Kevlar 11 (Ø 0.29 mm to 0.5 mm) • Stronger • easier to manipulate • Nominal tension x3 Solution at this stage All susbsequent tests successfully passed with larger Kevlar cords
VIBRATION TESTS - SUMMARY OF RESULTS Both units mounted PACS like. Only X axis tested Input spectrum Random [0 - 2000 Hz] 20 - 200 Hz : + 3 dB 200 - 250 Hz : 0.28 g2/Hz 250 - 2000 Hz : - 12 dB ≈ 8.06 G rms Sinus [0 - 100 Hz] : 30 G Lower levels RAL LOW TEMPERATURE TESTS SPIRE STM mounted with 0.29 mm Kevlar strings on evaporator side Low temperature : 82 K Frequency shift • Tests at room T : • Tests at 82 K : • Tests at room T Once units warm : But ∆ = 116 Hz NOTE : same signature after warm up at room T
FREQUENCY SHIFT ? Cold V test on STMs does not make sense • Structure = Ta6V (thermal contraction 1.5 10-3) • Kevlar strings (-3 10-3, new value at -1.7 10-3 since then) • Aluminum body for cooler heart (4 10-3) External strings ≈ 2.9 DaN Tensioning at room T 12 DaN At low T Internal strings ≈ 13.9 DaN
VARIATION OF RESONANT FREQUENCIES WITH TEMPERATURE tension dependent ? Hysteresis between tensioning - detensioning define a "dynamic" Young’s modulus in real situation Y300K = 38.7 TE-0.018 + 3.4 TE0.516(GPa) Assuming average fit for up and down (TE : tension in N) Real situation : string + pulleys
CRYOGENIC QUALIFICATION MODEL (CQM) Both CQMs qualified SPIRE : 290µm/500 µm strings PACS : all strings 500 µm
QUALIFICATION PROGRAM Thermal tests (HCR#1) 5 days 80°C bake out Thermal tests (HCR#2) Room T vibration tests Thermal tests (HCR#3) Thermal tests Nominal perf.
HEAT FLOWS - CRYOSTAT TILTED AT 60° Note : use of the full 120 mn for the recycling phase, to get a flowing power as low as possible at the end of the phase
CONVECTIVE EFFECTS - CRYOSTAT TILTING Possibly down to 14 mW
VIBRATION TESTS - CSL JULY 2-4 2003 Input levels
CSL CQM VTESTS (RT) - INSTRUMENTATION • Accelerometers : • two pilotes on adaptating plate • structure • evaporator cold tip • evaporator switch base • pump switch base
MAIN RESULTS No major failure (lost one wire on HS redunded - CQM PACS) [800 - 1500 Hz] [125 - 140 Hz] [300 - 360 Hz] [300 - 650 Hz] XX / YY : XX : resonant frequency YY : corresponding G (0.5 G excitation)
COOLING POWER CURVES - HEALTH CHECK REPORT No significant difference between HCR#1, HCR#2 and HCR#3 or rather results consistent within ± 5 mK HCR#1 - CQM PACS : Parasitics estimated at 12 µW ± 10% [Case 1.62 K level 0 - 2 K level 1] Prediction ≈ 10 µW
AUTONOMY TESTS Nominal conditions : L0 = 1.7 K - L1 = 4 K • First test with 10 µW applied load 45 hours @ 290 mK CQM SPIRE Not within predictions 35 hours @ 291 mK CQM PACS • tests with various applied loads Tests performed in same conditions every time 1/time versus Papplied m0.L = (Papplied + Pparasitics).time Straight line : m0 and parasitics m0: amount condensed / L: latent heat
AUTONOMY TESTS - MORE DATA • Extra parasitic of 8 to 10 µW • Cooler undercharged by 10% Analysis of data
EXTRA PARASITIC LOAD ANALYSIS - KEVLAR ? Remark : results eliminate possibility of parasitic coming from contact with snubber OK at least in the range [2 K - 10 K]
EXTRA PARASITIC LOAD ANALYSIS - KEVLAR & TITANIUM Cooler operated without strap between switch and evaporator Note : cycle limited to 2.2 K / 35 K From experimental data : 6.5 µW Predicted : 6.7 µW Parasitic load
LATEST RESULTS - CQM Reset to nominal (strap not gold plated) Nominal conditions : L0 = 1.7 K - L1 = 4 K With 10 µW applied load 47 hours @ 291 mK Analysis of data • Parasitic of 13 µW (predicted 14 µW) CQM PACS delivered to SAp November 6th
FUTURE ACTIONS Heat switch - FM/FS models • production of a batch (≈ 10) • selection of best ones for cold tip • thermal characterisation procedure revisited • improved strap ON going thinking • geometry ? • limit the heat flow in case of contact ? • strap : flexibility
KEVLAR TENSION HISTORY Note : CQM PACS not retensioned at delivery (SAp demand)