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Learn how drilling technology was evaluated in drilling a 4000m deep geothermal well in Kakkonda, Japan, to combat high-temperature formations using innovative methods and overcoming challenges of gas ejection.
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How did we drill 500 oC formation in Kakkonda JAPAN March 17, 2002 IDDP workshop Iceland
MajorProject Elements • FUNDS: Japanese Government (NEDO) • Duration: 1992-2000, WD-1 drilling 1994-97 • Main purpose: To delineate deep geothermal reservoir Drilling technology studies • To evaluate drilling technology (2) To obtain useful data for practical use • Planned Well Depth: 4000m • Expected F.Temp: 400℃
1994 1995 1996 1997 1998 km Side Track 1 9-5/8” Tie-back Stuck pipe 2 Set 7” Slot -P Prod. Test 3 Set Scab Liner & Corro. Test CSG Retrieve test CSG 4 3.729m Drilling History of WD-1
PDM MWD-tool Bit O-ring seal Mud dispersant 150-175 (oC) 150-175 140-170 ? 250 (weighted) 300 (unweighted) Temp. Limitationsfor drill tools & materials
MWD PDM Stator Rubber PDM Can’t be used above 150 oC
O-ring Seal Three-cone bit life decrease drastically above 150 oC operating Temp.
Borehole temp. changes with different operations Highest Temp. Cond. MTO MTI POOH DRG RIH
Mud Temp. In Pump Rate RIH speed Borehole Temp. TDS-Cooling Method 50oC 130 ?? 200oC ??
TDS(Top-drive Drilling System) Conventional Usages ・Work efficiency (can drill 27m, instead of 9m continuously) ・Prevent stuck pipe New Usage ・Cool BHA while RIH Water swivel Motor
Borehole Dynamic Survey Experiments Temperature Memory Tools
Trajectory correction with PDM & MWD 8-1/2 inch 2600m FT:350oC
Evaluation of the TDS-Cooling Method Bit Life Comparison With & without TDS-Cooling method
Economic Evaluation of the TDS-Cooling Method
How did we combat with HT-Formation ? • Get as manyTemp. info. as possible • Mud cooling system • TDS-cooling method • Re-injection well • Enough Water • Well organized group(both Drlg. & Sci.) • Perseverance
Mud-Cooling System Geo-Cooler Conventional Mud Cooler Pit
Mud DeteriorationWhat has happened • When well depth was 3451m (and below): • When we circulated mud at 2546m CSG shoe, 2100ppm CO2 gas came up. • At 3000m • 17300ppm CO2 gas • Flow-back at 10 l/min mud • While drilling • High CO2 gas mud returned
CO2 gas content vs Depth Well Depth (m)
Countermeasures • Quit using Polymer • Add Lime • Spot fresh water before POOH BHA Results: CO2 gas contents decreased from 10kppm to 2kppm
H2S Gas Ejection H2S gas content mud (>100ppm) returned when mud was circulated at 3,642m But H2S content decreased after 30 min circulation
Countermeasure • Closed re-injection system
Terminated Deepening the Well BECAUSE • Incapable of increasing mud density (High Temperature) • Risk of more gas ejection when encountered lost circulation zone
Drilling Research Items in Kakkonda Evaluation of 1.TDS-cooling method 2.Casing damage & CMT-bond (USI-Log) 3.MDW & PDM 4.Three-cone bit bearing (O-ring seal) • Multiple-stage-cementing method • Mud additives in HT-condition 7. Cooling effects by Mud-coolers 8. CSG Corro.Monitor while producingbrine
Casing Corrosion Test Scab-liner