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Business Improvement Techniques NVQ Level 2. The Team. Peter Ferns. Nigel Wright. Adam Shephard. John Cleall. Mike Harvard-Taylor. AISH Technologies. Electro-mechanical design and manufacture of ruggedized defence enclosures using a wide range of processes including:
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The Team PeterFerns Nigel Wright Adam Shephard JohnCleall MikeHarvard-Taylor
AISH Technologies • Electro-mechanical design and manufacture of ruggedized defence enclosures using a wide range of processes including: • Sheetmetal/fabrication/laser cutting • Spray shop & powder coating facilities • Machine shop • Mechanical Assembly • Electrical Assembly • Flat panel display assembly • Fibre optic manufacture
Why choose BIT Implementing BIT is designed to reduce: • Poor delivery performance • Department bottle-necks • Untidy work areas • Generate additional floor space to include new processes
Plan: Identification • Over cluttered • Un-used potential • Redundant machinery • Health & Safety hazards • Low morale
Planning • Role responsibilities • 5W’s & 1H • Brainstorming • Action planning
Communicating • Team meetings • Feedback from operators working in the area • Planning reviews
Do: Confirming Current State We decided that it would be essential to carry out an extensive 5S exercise in an area that would allow us to free up space for red-tagging and the storage of some WIP. It would also yield a floor space utilization opportunity of £7500.
Implementation • Red Tagging and catalogue • Create shadow boards • Purchase tooling • Encouraged employee involvement to drive change in methods and attitudes • Utilise cleared area • Introduce Standard Operating Procedures • Regular 5S audit
Check: Measure results Process Performance The process was re-timed with the tool boards in place, and it was now 2 minutes and 35 seconds, which compared to the ‘before’ state of 17 minutes and 37 seconds is a 93% improvement
Confirming New State • Outcome • Floor space realised and now re-deployed as a packaging and quarantine area • New tooling implemented to realise annual cost saving • 5S score improved by 1600% • Two new SOPs created, issued and displayed to help Standardise & Sustain 5S improvements Target • Realise Floor Space Utilization of £7500 • Implement new tooling methods to realise cost saving of £2250 • Improve 5S score by 300% • Confirm / re-write / amend SOP to reflect the requirements to maintain new state
Personal Achievements • How to structure a LEAN activity • Better communication skills • The importance of involving those working in the areas chosen for the business improvement • Problem solving techniques • Understanding and working with personalities within the team • Spreading the philosophy of the process